Methodology
Ventilation and odor control used:
Introduced fresh air into pipe past downstream plug through downstream and mid-point manholes by exhausting air from upstream manhole.
Rehab method used:
Danby Panel Lok III-E spiral wound into the pipe with a finished diameter of 84” with full annulus grouting with cementitious grout with minimum compressive strength of 6,000 psi.
Cleaning method used (if required) and who cleaned the line:
High pressure (6,000 psi) water blasting performed by Danby installer, Boyer, Inc.
Method of flow bypass or diversion, if used:
Downstream inflatable plug to prevent backflow from tidal influenced river outlet and upstream sand bag weir with 2” submersible electric pump to bypass small base flow. During storm events, sewer was evacuated and downstream plug was deflated.
Hurdles
Problems encountered during construction:
Heavy rains delayed work progress, curves in pipeline and large manhole with spring line shelves required customizing panel installation. Large diameter required greater care in grouting to avoid deforming liner (no separate bracing was used to support liner). Cement and fly ash supplier had QC problems in his plant which necessitated removal and replacement of substandard grout. Material supplier changed.
Problems encountered after construction:
None.